BABYLOCK SERGER SLOWS DOWN REPAIR links

BabyLock sergers are fantastic, especially the all metal (except plasticfaceplate and tension knobs), but like all mechanical items, they can slow down with age.






If the motor runs fine, without the belt attached to the handwheel, these vintage BabyLock sergers have one area thatjust needs a little extra care, to get it back in good running shape! There are 2 metal bushings, of 2 different types of metal, so over time, they build up metal burrs, which make it so they slow the serger down, as soon as it warms up!

"Due to the disparate metals of the stitch length eccentric cam and linkage, the clearance between the two parts diminishes. The lighter colored cam has to be extracted and polished with emery until the cam spins freely in the linkage bore." Wayne Pedersen

Here is a link to instructions for repairing it-

BabyLock serger hand wheel hard to turn



Babylock Serger slows down hard to turn handwheel repair info

I am including photos of other instructions I printed out, for repairing sergers, for myself, as well as others!


Serger repair information photos


Andy Ruina Feb. 17, 2020 on Facebook Sewing Machine Collect & Repair Lounge

"Successful Babylock Serger repair. BL4-736D. This is a four thread serger from 1970 or 1980 or so. Made by Juki.

Symptom of Problem: Makes a good stitch, runs well for about 10 seconds and then slowly grinds to a halt. Let it rest and the problem repeats.

I don't know how or where to post this so that people can find it. I am posting that which I wish I could have found before. Over the years, here and there on the internet, others seem to have had this problem. I did find the solution below, I don't remember where, but I didn't understand it until I did it myself.

Short version of the solution. Take off the left side of the cover and the machine bottom. At the left side of the machine is a stitch length regulator. Pry off (with a knife) the plastic cap on the cover(with an arrow marked on it). Unscrew the big screw that is revealed. Pull apart that which you can. There is a round piece, about 1" diameter, that slides in a round hole. That piece was tight in that hole. With fine grit sandpaper and a dremel tool grind the two pieces down until they slide easily in each other. Grease and reassemble. We also had to adjust the feed dog timing by unclamping that same piece from the main shaft, and turning until the feed dogs were moving cloth only when the needles were out.

It stitches neatly, smoothly and fast after this repair.

How did we locate the problem? First we loosened the the rotating parts for the feed dog from the main shaft. The motor then ran tirelessly. So the problem is/was somewhere in the feed dog area. Then we reclamped the rotating feed-dog stuff to the main shaft. Then we set the stitch length to zero, so all the feed-dog stuff wasn't moving. And the problem returned. Thus the problem had to be in the part that connected the main shaft to the feed dog stuff because that was the only thing sliding in that general area of the machine.

Because we are lucky, that part is at the protruding end of the main shaft and all comes apart easily once you take off the plastic cap and unscrew that main screw (the one under the plastic cap).

The cam, that eccentric sliding part, was quite jammed, so taking it apart took some little effort, pushing on one side or another. But then it came apart. And dremmeling and sand paper got it so it could go again together and turn without jamming. And grease made it so it would slide smoothly.

What caused the problem? The consensus seems to be that the machine must have sat for a few decades unused, with lubricant evaporating out. Then it was run too hard and too fast and too long. Then the parts got too hot and either galled (metal melting on metal) or got distorted. We couldn't see any galling.

Besides the covers, this repair only involved removing a single screw. And, to get the feed dog timing, which was messed up in the diagnosing phase, we had to loosen and tighten two set screws to the main shaft.

In the end, if I had to do the identical repair again, and no diagnosing, the whole thing would be about 1/2 hour. No complicated disassembly. And only one simple timing adjustment.

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I realize that everytime anyone fixes anything they have an adventure like this. So there are 10,000 potential tips like this out there for 1000 different machines. But it is nice finding tips on the internet. So I leave this one for someone else to find.

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I am still hoping for ideas about where to get information like this about sergers. Mark Sumpter wrote a great introduction to serger stitches. Now we (I) would like some information about the machine(s)."




Another site for serger repair information is She'saSewingMachineMechanic


BabyLock Pro Line 838D

BABY LOCK BABYLOCK 5360E

INFORMATION ON BUSHING REPAIR BLOGS

Baby Lock Babylock BL4-736




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